Linkedin article banners (6)

Reducing Process Weight Variation Using Six Sigma DMAIC Approach

Executive Summary

A process improvement initiative was undertaken to reduce weight variation in a manufacturing process. The baseline variation was ±20g, leading to high rejection and rework costs. Using the DMAIC methodology, variation was reduced to ±8g, improving process capability and reducing cost.

Problem Statement

The process exhibited inconsistent output weight beyond acceptable tolerance limits, resulting in rejection, increased material consumption, and customer dissatisfaction.

Project Goal

  • Reduce weight variation within defined tolerance
  • Minimize rejection and rework

Business Impact

Metric Before After Improvement
Weight Variation ±20g ±8g ↓ 60%
Rejection Rate 5.5% 2.1% ↓ 62%
Rework Cost ₹3,00,000 ₹1,20,000 ↓ 60%
Cpk 0.85 1.45 Improved

Define Phase

  • Identified weight inconsistency as critical defect
  • Defined CTQ: Product Weight
  • Mapped process flow
  • Stakeholders aligned

Measure Phase

Initial data collection indicated high variability in process output.

unnamed

Analyze Phase

Category Cause
Machine Temperature fluctuation
Method Improper parameter settings
Material Inconsistent material mix
Man Lack of standard operating procedure
Environment Cooling variation

Process instability was confirmed using control charts.

unnamed (1)

Improve Phase

Actions Implemented:

  • Standardized temperature profile
  • Controlled material mixing ratio
  • Fixed cooling system inconsistencies
  • Implemented parameter checklist
  • Operator training

unnamed (2)

Control Phase

Control measures, including SOPs, monitoring systems, and periodic audits, were implemented to sustain improvements.

Conclusion

The Six Sigma DMAIC approach successfully reduced weight variation and improved process capability, leading to significant cost savings and quality improvement.

Leave A Comment

All fields marked with an asterisk (*) are required

Social media & sharing icons powered by UltimatelySocial